lcd_encoder was int32_t (4 bytes) because of the menu code
when editing through the menus, the menus only accept
int16_t so it doesnt make sense to use int32_t.
Change in memory:
Flash: -892 bytes
SRAM: -2 bytes
This change needs to be approved of course due to it affecting UI
The affect UI is only one menu
lcd_settings_linearity_correction_menu
I doubt many users are using this menu except very advanced users.
I propose we delete the variant of menu_draw_P which was used for
uint8_t but renders them as floats.
Instead treat
uint8_t same as int16_t i.e. just render integers.
Keeping it simple :) Solve our fanSpeed problem.
Change in memory:
Flash: -140 bytes
SRAM: -2 bytes
These variables only range from 0 to 255
For the menus we currently need to convert fanSpeed to int16_t.
Change in memory:
Flash: -160 bytes
SRAM: -2 bytes
This fixes the spurious feedback when rotating the knob
because lcd_update is called much often than the interval
at which the lcd rendering is updated
Change in memory
Flash: -88 bytes
SRAM: -9 bytes
This commit adds the ability for firmware to make sounds when the
knob is clicked or rotated, when LCD updates are disabled.
The improvement here is the sound is being made with one line of code
whether or not LCD updates are enabled or disabled.
Change in memory:
Flash: -24 bytes
SRAM: 0 bytes
Valid values range from -100 to 100. Storing this value as four bytes
(int32_t) is not efficient.
Instead we can store G80 user input temporarily as int32_t and check
if the value is within the allowed range. If it is, then we convert the
int32_t (4 bytes) to int8_t (1 byte).
Change in memory:
Flash: -78 bytes
SRAM: 0 bytes
This way doesn't add any more flash memory.
Calculating the string length or checking for a null byte
will end up increasing flash consumption overall.
This gets rid of float conversion.
We just need to check the 6th character when M862 is detected. This
character gives us the digit after the dot.
Change in memory:
Flash: -20 bytes
SRAM: 0 bytes
For non-time critical code it is more effcient to call a function
rather inlining each division operation.
Change in memory:
Flash: -122 bytes
SRAM: 0 bytes
Rename acceleration_st to acceleration_steps_per_s2 to be same as Marlin 2
Store the accelerator in local variable accel
while we are performing the limit checks.
When limit checks are done we can assign
the block it's acceleration. Especially
block->acceleration_steps_per_s2 is now only written to once, instead of direcly in the limit checks.
Change in memory:
Flash: -118 bytes
SRAM: 0 bytes
Noticed this when exploring another optimisation
By specification exactly which overloaded function to use
we save some memory
Seems to have something to do with doing arithmetic in the function argument
Change in memory:
Flash: -156 bytes
SRAM: 0 bytes
Currently we are queuing many small 2 mm E-moves until the filament
sensor triggers. We do this because we never abort any queued moves,
so making small 2 mm moves ensures we do not move the E-motor more than
2 mm past the filament sensor.
Unfortunately, when E-cool mode is enabled, the E-motor will create
audible clicking sounds (similar one hears during jam or a loose grub
screw). A workaround for this is to queue one or more very long moves.
Where very long is something of the order of hundreds of millimeters. I
have it set to 350 mm but it's just a random constant really. Keep in
mind the firmware will block too large E-moves, if I recall correctly
it was anything above > 450 mm (see PREVENT_LENGTHY_EXTRUDE)
In order to use very long moves, we must somehow stop the E-motor from
moving once the filament sensor triggers. In other words, throw away
what's left of the current E-motor move. For this simple purpose we can
use planner_abort_hard() but we must set planner_aborted to false
afterwards because the code architecture does not allow the main loop()
to run until the Toolchange command is done processing.
Change in memory:
Flash: +18 bytes
SRAM: 0 bytes